The EIA reported the first withdraw of the season of -134 Bcf which was much higher than the predicted -113 Bcf.  Last year’s withdraw was -42 Bcf and the 5-year average is -25 Bcf.  Today’s withdraw widened the storage deficit …

SummerRR

The EIA reported today a net gas withdraw of -183 Bcf for the week ending January 12, 2018, which was less than the market predicted -199 Bcf.  The withdraw was also lower than last years withdraw of -230 Bcf and …

SummerRR

The EIA reported a net gas storage Withdraw of -359 Bcf for the week ending January 5th 2018. This was quite a bit larger than the market consensus of -333 Bcf. The withdraw is significant because it’s the largest …

SummerRR

The EIA reported a net gas storage INJECTION of 2 Bcf for the week ending December 1, 2017. This was bearish to market expectations which were centered around a 3 Bcf withdraw. A year ago, we saw a withdraw of …

SummerRR

The EIA reported a net gas storage injection of 15 Bcf for the week ending November 3rd, right in line with the general consensus.  The Nymex prompt month is trading relatively flat to the open at $3.27. Storage …

SummerRR

The EIA reported a net gas storage injection of 64 Bcf for the week ending Oct. 20, 2017.  This was close to the general consensus of 65 Bcf.  The Nymex prompt month is trading down -$.035 to $2.89 MMBtu.  Storage …

SummerRR

The EIA reported a net gas storage injection of 53 BCF this morning with the week ending August 11th, 2017. This week’s report was above the market’s expectation which was centered around 48 BCF. Storage stands at 3,082 BCF which …

SummerRR